Southern Pacific #18 Restoration – April 2014

The weekend of April 12th and 13th was to be the weekend for the final push to lower the #18 back onto her driving wheels. By the end of the day on the 12th after a year and a half the #18 was back on her wheels.

Finally back on wheels after a year and a half.
Finally back on wheels after a year and a half.

There was only about 6″ further to lower the locomotive. Just as before we had to lift, remove cribbing, and then lower and reset the jacks, while in between checking the driver boxes and making adjustments as needed. Shortly after we began lowering we had to re-install the remaining spring rigging for the #3 drivers. Because of tight clearances, and issues with the rear springs and driver boxes this was a difficult job.  After some sweat and hard work we got them in.

Getting ready to lift and lower.
Getting ready to lift and lower.

 

Making adjustments to the driver boxes.
Making adjustments to the driver boxes.

At the front end things were a little easier with the pony truck. We removed the cribbing, double checked the alignment of the bolster then lowered the locomotive into the pony truck.

Once down far enough for the frame to clear the bottom of the driver boxes we installed the frame binders, and ran the wedges up. The latter of which will be properly adjusted later. Finally it was all clear to lower her down all the way. Once down we made note of any issues and took some measurements for later reference. It was found that the locomotive was still not sitting quite right and that we will have to build up at least two of the spring saddles to accommodate for the crown brass and axle work.

Partially out side for the first time in four years.
Partially out side for the first time in four years.

 

On Sunday it was decided that it would be best to roll the locomotive as far as possible in hope that she would settle with the drivers and the driver boxes with the frame. While prepping for this move, copper ferrell’s for the tubes were being installed in the front tube sheet.

When we where ready to move, we hooked her up to a jeep with a winch and pulled backwards until the back end was outside the tent. This was the first time she had been outside the tent since 2011. Then we pushed (with man power) her back in. As planned, this did align the locomotive and wheels.

18 moved back to help align the wheels and driver boxes.
18 moved back to help align the wheels and driver boxes.

 

 

 

As before THANK YOU to all who came out to help. This was a big step towards completing the restoration. It sure is good to see her on her wheels again.

 

 

In other news we now have available for purchase a limited edition 13×19 print of Jan Rons painting of the #18 at our proposed engine house. Details can be found by following the link on the upper right side of the page.

2013_0724CCRwyArtwork0004a

 

 

Southern Pacific #18 Restoration – February and March 2014

The period between the 13th of February and the 3rd of March will undoubtedly go down as a major mechanical turning point in the restoration of the #18. It will also be remembered as a period of some of the hardest work we have performed; by the numbers that means over 2000 miles driven to get the drivers in Washington and over 800 volunteer hours spent in Independence over two weekends. While the full story would be worthy of any reality TV show (or our newsletter), the end result was that Dave, Rick and Forest – despite a few flat tires, rain, a broken axle, and a helpful guy named Lucky – were able to retrieve the drivers at the Mt. Rainier Scenic RR between Feb 13th and 17th. Stathi and his crew at MRSRR did a great job at rebuilding the drivers.

CMO of the Mt. Rainier Scenic RR, Stathi stands with one of our drivers.
CMO of the Mt. Rainier Scenic RR, Stathi, stands with one of our drivers.

With the drivers back in Independence, the subsequent work over the weekends of the 23-24th and March 1-2nd have put the locomotive back on the rails…..almost.

The big pushes on the 23rd and 24th were to unload the drivers, get the driver boxes assembled on the axles with new grease cakes and most importantly, complete the layout and machining of the shoes and wedges, know as tramming.

Unloading the drivers. so work can begin
Unloading the drivers. so work can begin
Travis and Dave setting a driver on the rails.
Travis and Dave setting a driver on the rails. Feb 23rd.
The driver boxes are all sitting ready to receive the final grease grooves and be installed on the axles.
The driver boxes are all sitting ready to receive the final grease grooves and be installed on the axles.
The finished job, all the boxes ready to go with the grease cellars repaired and repacked. Note the new axle on the #3 driver farthest away in the photo.
The finished job, all the boxes ready to go with the grease cellars repaired and repacked. Note the new axle on the #3 driver farthest away in the photo.

 

 

 

 

 

 

 

 

 

 

 

 

 

 

Aside from the driver prep work, we also installed the steam dome lid, finished the left boiler check valve and installed all the boiler plugs. All that’s remains is to roll the tubes in place and fill the boiler with water. Marty and Scott spent most of the weekend lapping the right valve in place. Aside from some quick machining the valve is about together.
With things more or less ready to go, a group of a dozen volunteers arrived for the big weekend of March 1st and 2nd.

First off, thanks need to go to the Virginia and Truckee Railroad for kindly loaning us their four Duff-Norton high lift pneumatic jacks for the weekend.

After spending a few hours taking care of a couple small items that were missed the previous weekend it was time to lift, and lower. The first job was to go up one lift to have the engine high enough for the drivers to clear as well as remove the frame binders which go under the frame openings.

Clear track and getting ready to lift.
Clear track and getting ready to lift.
As high as we need to be with the locomotive.
As high as we need to be with the locomotive.
The drivers are in place and the engine is coming back down.
The drivers are in place and the engine is coming back down.
With it past dinner time on Sunday, the engine is almost back to earth and on the wheels.
With it past dinner time on Sunday, the engine is almost back to earth and on the wheels.

Once the wheels were rolled in place, the engine was slowly lowered back down, and that’s when the frustrations started. During the process of lifting and lowering the engine for the removal of the wheels the engine had shifted about 3″ to one side of the rail line, before things could go back together it had to be shifted back over. To do this safely with the engine on jacks was a chore. The jacks were set at a slight angle and the engine was repeatedly lifted and lowered to inch it over, once close, the engine was then lowered over the wheels and small hydraulic jacks were used to push it the last 1″ into alignment. All totaled, it took the crew until about 9pm Sunday night to have the engine back down and almost in place, it is still blocked up about 4″, or just above the point of where the spring rigging will begin to take the weight.
As if all the locomotive work wasn’t enough, a few guys worked over at the museum inventorying rail and track components as well as moving out scrap iron in an effort to get the new museum site ready for track later this year.

Finally, a big THANK YOU to everyone who has helped over the course of the month on this big project, we couldn’t have done it without you!

Some of the crew that made this all possible enjoying another Independence lunch.
Some of the crew that made this all possible enjoying another Independence lunch.