Southern Pacific #18 restoration-March 2015

On the weekend of March 28-29 a good number of us gathered once again to tackle more work on the #18. On the list of jobs to do was to install the firebrick, finish fabricating and install the petticoat mounts, cut and install more boiler jacketing, finish plumbing and then mount the burner, and last but not least build some panel track so we can roll the #18 out of the tent far enough to set the sand dome atop the boiler.

Marty helping Scott with trimming and installing the firebrick.
Marty helping Scott with trimming and installing the firebrick.
Firebrick in the fire box.
Firebrick in the fire box.

Everything on that list was accomplished. Scott and Marty spent the majority of both days laying out and installing the firebrick in the firebox. This required lots of fitting and chipping and refitting. The firebrick has several functions, it insulates the firebox sheets from the direct heat of the fire, stays hot (glowing red) after the fire is out which helps slowly cool the firebox, and if the fire accidently goes out the red hot brick will relight the fire. A special type of high heat mortar is used to hold the brick in place.

Working down under the locomotive, Mike and Ryan finished up the remaining plumbing for the burner. After some cleaning and wrapping the plumbing in insulation, it was all ready to go back on the engine along with the burner.

Forest and Rick meanwhile worked on cutting and fitting the new boiler jacketing. This is a pretty straight forward process of tracing the old jacket sections and cutting the new ones. Simple but time consuming, and even after you copy the old jacket sheets they always seem to need more trimming. After the sheets were cut they were put in place and the brackets installed to clamp them in place.

Jeff working on the petty coat.
Jeff working on the petty coat.

Up front in the smoke box I began assembling and welding the new petticoat pipe mounts. These are different from the originals in that they will be adjustable. Adjustment of the petty coat may come later after the engine has been steamed up and run. If the petticoat is not at the right height above the blast nozzle it can affect the draft in the boiler.  On Sunday, Gary finished the assembly and welding of the mounts. Next time we will work on the baffles and should also be able to reinstall the smokebox door.

Mike and Ryan working on the panel track.
Mike and Ryan working on the panel track.

While all this was going on Dave was gathering rail to assemble the panel track. After finishing the burner, Mike and Ryan helped assemble the track. To accomplish this meant torching the rails to the same length and cutting holes in them for splice bars and all thread to hold the rails at the correct gauge.

Modified 64 rod brass
Modified 64 rod brass

Beyond the weekends work, we also took delivery of the new rod brass billet. Modified-64 brass is the standard material to use with locomotive rod brasses and crown brasses. With the material on hand we are now headed towards getting the new brasses made and the rods installed. To help us facilitate  final machining of the new bushings we now also have a new home for our lathe and mill. Joe Andrews our long time machinist and 50 year Independence resident is moving to Oregon and so we had to move our machine shop to a new location. We will miss Joe, but we have a great new building for the tools.

Our new machine shop
Our new machine shop

Over at the museum, trackage and dirt work plans are being currently reviewed by the County public works department. Once stamped we can proceed with the dirt and track laying. We have also begun the process of getting building quotes and pricing. Things at the museum are moving forward, a little slowly perhaps, but forward none the less.

And lastly, Ed Fleming our official videographer has put together a quick little piece on the bell installation from February. You can check it out here.

 

Southern Pacific #18 restoration – February 2015

The new reservoirs drilled and ready.
The new reservoirs drilled and ready.
Rick shows off the finished lube lines.
Rick shows off the finished lube lines.
Travis and Randy lagging away.
Travis and Randy lagging away.
The lagging continues.
The lagging continues.
Marty and Randy mudding the first courses.
Marty and Randy mudding the first courses.
Travis is giving a final lap on the throttle.
Travis is giving a final lap on the throttle.
Sometimes skinny pays off. Travis installing the throttle.
Sometimes skinny pays off. Travis installing the throttle.
Marty tightens down the dome lid.
Marty tightens down the dome lid.
Marty getting the doughnuts ready for installation.
Marty getting the doughnuts ready for installation.
Dave and Marty lying around.
Dave and Marty lying around.
Everyone waiting for Marty.
Everyone waiting for Marty.
Doing the final tightening on the seats.
Doing the final tightening on the seats.
The engineers injector loosely in place.
The engineers injector loosely in place.
In comes the bell.
In comes the bell.
Fitting the bell and roughing in the jacketing.
Fitting the bell and roughing in the jacketing.

bell 20150220_151945

February may have only 28 days, but we managed to work 8 of them over the course of two weeks.

The first work week was three days that focused on drilling the new reservoirs and installing the lube and air lines. The reservoirs are newly built and certified, and along with the process of drilling them with a series of very shallow holes, allows them to not require annual testing per FRA regulations. This is the same practice on modern diesel locomotives. The lube lines, and air lines, are four lines that run from the cab under the insulation to the valves, air sanders on the sand dome, and bell ringer. These lines all had to be bent into position, threaded and, the copper flared and annealed.

After making tremendous progress with a small crew, a larger crew was on the job the following week for almost five full days. There were multiple areas of focus over the week, perhaps the most noticeable work was lagging the boiler. Installing the insulation, or lagging, is a dirty job that at one time would have been done with asbestos. Today we use calcium silicate block and mud. Utilizing the heavy wire we had previously wrapped around the boiler barrel we started at the front bottom and worked our way up and around wiring the block with light gauge stainless steel wire to the existing wire. Some areas were easy with full blocks, while some areas required custom cut pieces. After about 16 hours with three of us cutting, wiring, and measuring we had the entire boiler barrel complete (the cab and wrapper sheet areas will not be lagged until after the first steam up) and ready to mud all the rivet and pipe areas. It was exciting to see a different looking locomotive after all these years looking at a red primer boiler.

Before we had lagged the area around the dome we had our FRA inspectors in town to perform their post hydro interior inspection. All went very well with the inspection and we were able to re-install the throttle and the dome lid. This was their last inspection prior to the engine being steamed up.

Before putting the throttle back in we did a bit more lapping on it since we had discovered it leaked some during our previous hydro test. After lapping, it was then time to install the throttle, which, as we have come to find out is about the most difficult job on this engine. Travis kindly volunteered and squeezed into the dome to do the install. Hours later, the dome was installed and we performed yet one more hydro to make sure our previous re-sealing of the dry pipe joint on the front flue sheet was not leaking, thank goodness it wasn’t, or we may have given up the entire project in frustration.

With the dry pipe not leaking, we moved onto our other big – or at least heavy – job, installing the steam pipes in the smokebox…yet again. Thanks to the aforementioned dry pipe joint that was leaking we had to remove the pipes after our first install, did I mention they weigh about 300 pounds each. At least we were experts at doing it and this time it took only about 2 hours to have them both in and seated in place. The firemans side proved to be a bit tricky since the newly repaired ears were just slightly off of the correct angle.

With pipes in we then hydro tested them through the slide valves to make sure the joints were all sealing, which they were, with the exception of one that required a little more tightening.

Aside from the bigger more photogenic projects mentioned above, there were also many other important things occurring such as cleaning up the fire bricks (these were new bricks installed in the 90’s but the loco was never fired with) and prepping them for re-installation, installing some of the below cab floor air lines and brackets, and also fitting the injectors and their brackets and plumbing.

On our final day of work, after the insulating mud had dried we began to fit the new (old) jacketing. The jacketing was built in the mid1990’s when the asbestos and original jacketing were removed. While in generally good condition, it will require replacement of some pieces and refitting of others. To correctly fit the jacket we had to re-install the bell and lower steam dome rings.

For next months work we can now continue on with installing the petticoat pipe in the smokebox, install the firebrick and sand dome as well as continue on with the jacketing. Slowly but surely we are getting closer and closer to steam!

Finally, we received a new boxcar! Well actually it was delivered back to us from Olancha where it had been living. #451/13 is honestly in the best condition of the 3 boxcars currently at the museum. Currently we have no plans to do anything with it other than set it up for storage. Someday we would like to make one boxcar serviceable for behind the #18 at the museum and this may be the one.

As always a big THANK YOU to everyone that comes to work as well as everyone that helps house and feed those who do come from out of town, we couldn’t do it without you!!

Bob and Scott are cleaning up the fire bricks.
Bob and Scott are cleaning up the fire bricks.
Our new boxcar #13
Our new boxcar #13